Transcript Document
MGPA test results first results presented 25th June – repeat here + some new results testing begun 29th May on bare die (packaging still underway) two chips looked at so far – both working (all results here from one only) OUTLINE introduction test setup description analogue performance gain linearity matching noise (barrel and endcap) 5 Mrads irradiation results I2C offset adjust calibration feature power consumption summary 9th July, 2003 CMS Ecal MGPA test results 1 MGPA target specifications Parameter Barrel End-Cap fullscale signal 60 pC 16 pC noise level 10,000e (1.6 fC) 3,500e (0.56 fC) input capacitance ~ 200 pF ~ 50 pF output signals (to match multi-channel ADC) differential 1.8 V, +/- 0.45 V around Vcm = (Vdd-Vss)/2 = 1.25 V gain ranges 1, 6, 12 gain tolerance (each range) +/- 10 % linearity (each range) +/- 0.1 % fullscale pulse shaping (filtering) 40 nsec CR-RC channel/channel pulse shape matching <1% 9th July, 2003 CMS Ecal MGPA test results simulation results OK for mid and high gain ranges (low gain not a problem) technology spec. for resistors used OK OK 2 transconductance gain stages MGPA main features diff. O/P stages 3 gain channels 1:6:12 differential outputs -> multi-chan. ADC pulse shaping (external components) RfCf = 2RICI = 40 nsec. I2C interface to programme: output pedestal levels enable calibration feature cal DAC setting CI RI RG1 RI CI RI ext. trig. CCAL RG2 charge amp. CI RI RG3 I/P RI RI Rf Cf 9th July, 2003 VCM DAC choose RfCf for barrel/endcap calibration facility prog. amplitude (simple DAC) needs external trigger I2C and offset generator CMS Ecal MGPA test results 3 VCM VCM MGPA photo offset gen. die size ~ 4mm x 4mm I2C for packaging in 100 pin TQFP diff. O/P stage hi VI stage mid charge amp lo 9th July, 2003 CMS Ecal MGPA test results 4 RAL test board packaged chips not yet available but RAL board can take bare die dual purpose design 1) standalone–used here 2) interface to standard DAQ system bias components fixed – no adjustment possible (without changing 0402 components) most results here for barrel feedback components to first stage (except where indicated) 9th July, 2003 CMS Ecal MGPA test results 5 Test setup for pulse shape measurements diff. probe or singleended buffered signal note: very fast risetime charge injection -> pulse shape distortion on rising edge due to slew rate limitation at O/P of first stage current source magnitude OK for 10 nsec exponential edge O/P I/P Scope averaging -> 16 bit resolution. Multiple waveforms captured with different DC offsets to remove scope INL effects. 9th July, 2003 CMS Ecal MGPA test results first stage amplifier 6 Pulse shapes – low gain channel signals up to 60 pC (feedback components for barrel application: 1.2k//33pF) steps not equally spaced (log attenuator) 2 active probes on +ve and –ve outputs (before any buffering) linear range +/- 0.45 V around Vcm (1.25 V nom.) note: Vcm defined by external pot’l divider (5% resistors) so not exactly 1.25 V 9th July, 2003 CMS Ecal MGPA test results 7 Pulse shapes – all 3 gain ranges 9th July, 2003 CMS Ecal MGPA test results 8 Differential pulse shape – low gain channel differential probe on chip outputs (before buffering) 60 pC fullscale signal as before differential swing +/- 0.45 V around Vcm corresponds to ~1.8 Volt linear range pedestal subtracted no “obvious” pulse shape distortion due to higher gain channels saturating 9th July, 2003 CMS Ecal MGPA test results 9 Differential pulse shapes – all 3 gain channels compared – gain ratios 1 : 5.6 : 11.3 (cf 1 : 6 : 12) no obvious interchannel distortion effects 9th July, 2003 CMS Ecal MGPA test results 10 Linearity and pulse shape matching – high gain channel fullscale signal 5.4 pC pulse shape matching in spec., linearity outside by factor ~2 9th July, 2003 CMS Ecal MGPA test results 11 Linearity and pulse shape matching – mid gain channel fullscale signal 10.8 pC smallest signals show slower risetime – needs further investigation 9th July, 2003 CMS Ecal MGPA test results 12 Linearity and pulse shape matching – low gain channel fullscale signal 61 pC similar (but worse) effect as for mid-gain channel 9th July, 2003 CMS Ecal MGPA test results 13 Pulse shape matching between gain channels Pulse shape matching definition: Pulse Shape Matching Factor PSMF=V(pk-25ns)/V(pk) spec. Pulse shape matching = [(PSMF-Ave.PSMF)/Ave.PSMF] X 100 Ave.PSMF = average for all signal sizes and gain ranges systematic discrepancies between channels can be due to mismatch in diff. O/P termination components or (more likely here) difference in stray capacitance from PCB layout 9th July, 2003 CMS Ecal MGPA test results 14 mismatch of stray O/P capacitance likely due to signal routing on test card 1st stage of buffering differential O/P termination components (1% tolerance) 9th July, 2003 CMS Ecal MGPA test results 15 effect of input capacitance on pulse shape pulse peak shifts by only ~ 3 nsec. => robust to variations in stray capacitance 9th July, 2003 CMS Ecal MGPA test results 16 Noise measurements use wide bandwidth true rms meter (single ended I/P) => need diff. to singled ended buffer circuitry => extra noise contribution to subtract will also add extra noise filtering Barrel (33 pF // 1.2k) Endcap (8.2 pF // 4k7) Cstray (~20 pF) Cstray + 180 pF simulation 200 pF Cstray (~20 pF) Cstray + 56 pF simulation 50 pF high 7,000 7,850 6,200 2,900 3,050 2,700 mid 8,250 9,100 8,200 3,300 3,450 3,073 low ~ 28,000 ~ 28,000 35,400 ~ 8,500 ~ 8,500 9,800 endcap results NEW weak dependence on input capacitance as expected estimated errors: ~ 10% high and mid-gain ranges, ~ 20% low gain range (buffer circuitry dominates here) 9th July, 2003 CMS Ecal MGPA test results 17 Radiation results: pulse shape low mid high pre-rad 5 Mrads 10 keV X-rays (spectrum peak) , dosimetry accurate to ~ 10%, doserate ~ 1 Mrad/hour, no anneal as yet ~ ½ fullscale signal injected for each gain channel ~ 3% reduction in gain after 5 Mrads 9th July, 2003 CMS Ecal MGPA test results 18 Radiation results: noise Cstray + 180 pF Cstray + 180pF +5 Mrads simulation (200 pF) high 7,850 7,250 6,200 mid 9,100 8,700 8,200 low ~28,000 ~32,000 35,400 no significant change (within errors) after irradiation 9th July, 2003 CMS Ecal MGPA test results 19 Radiation results: linearity & pulse shape matching high gain channel shown here linearity degraded slightly at extreme edge of range 9th July, 2003 CMS Ecal MGPA test results 20 I2C pedestal offset adjustment high gain channel shown here (other channels similar) I2C offset setting 0 offset setting 0 -> 105 in steps of 5 (decimal) linear range ~ optimum baseline setting here corresponds to I2C setting ~70 I2C offset setting 105 9th July, 2003 CMS Ecal MGPA test results 21 external Calibration circuit functionality (1) 10k 1nF high on-chip 8 – bit DAC value 0 – 2.5 V Rtc 10pF MGPA I/P derived from external pulse mid low distortion on rising edge for low gain channel – somehow related to external 1 nF cap. 9th July, 2003 CMS Ecal MGPA test results 22 external Calibration circuit functionality (2) with 1 nF without 1 nF 10k 1nF on-chip 8 – bit DAC value 0 – 2.5 V Rtc 10pF MGPA I/P calibration pulse shapes with/without external 1 nF show improvement if removed effect needs further investigation 9th July, 2003 CMS Ecal MGPA test results 23 main concern so far: high frequency instability (~ 250 MHz) can be introduced on first stage O/P when probing not clear whether problem on chip (no hint during simulation) or could be test board related decoupling components around first stage not as close in as would like VDDP, VS in particular test board for packaged chips should help with diagnosis decoupling closer in (may be cure?) bias currents easy to vary (should give clues) new version of this board also in pipeline will also take test socket 9th July, 2003 CMS Ecal MGPA test results 24 Power consumption Current measured in 2.5 V rail supplying test board -> ~ 245 mA -> chip current + Vcm divider (4mA) + power LED (3mA) chip current = 238 mA measuring bias currents and multiplying by mirroring ratios -> 235 mA may change if further testing indicates changing bias conditions -> performance improvements worth having 9th July, 2003 CMS Ecal MGPA test results 25 Summary all results so far for one unpackaged chip, barrel feedback components to first stage gains close to specification (1 : 5.6 : 11.3) pulse shapes good linearity ~ +/- 0.2% (~ 2 x spec.) pulse shape matching within spec. apart from lowest end of mid and low gain ranges no obvious distortion introduced on lower gain channels by higher gain channels saturating => good chip layout noise close to simulation values (< 10,000 (3,500) e for mid and high gain ranges for barrel (endcap)) I2C features (channel offsets, calibration) fully functioning 5 Mrad radiation results – small effects only for more detailed studies need packaged chips 9th July, 2003 CMS Ecal MGPA test results 26 MGPA – architecture overview external components define CR and CSA gain V/I gain resistors diff. O/P external components define RC offset adjust I2C interface 9th July, 2003 offset & CAL pulse generation CMS Ecal MGPA test results 27 9th July, 2003 CMS Ecal MGPA test results 28